| Yesterday, 10:33 AM | #90 |
|
Second Lieutenant
![]() 31
Rep 200
Posts
Drives: 2015 435i Gran Coupe
Join Date: Dec 2014
Location: Plano, TX
|
Morning,
I am trying to understand the following log and pinpoint my problem. Car information is below 2015 F36 xdrive 8at EWG Dinan Cold Air intake ER Chargepipe Upgraded intercooler VRSP TIC Pipe MST turbo inlet pipe Catted down pipe MPExhaust Dorsch Stage 1 HPFP Upgraded LPFP 3.5bar TMAP Turbosmart Blow off valve Spark Plugs at .0021 Pure 500 turbo Tune with Cary Jordan or E50 blend I have done a smoke test and eventually boost test. I changed out the o rings on : CP to IC Turbo to TIC TIC to Intercooler Cleaned up the bov o rings I did a boost test on Friday and noticed air coming from the copper opening on the turbosmart blow off valve. i thought it was dirty and took it out and cleaned it up. Sidenote( I know taking that blow off valve is a pain in the ass. I wish i did the following from the beginning: remove the Turbo inlet pipe, that paired with a 5 mil balled headed socket would have saved me hours (like 4 hours easily of trying to get the right angle) Based on my logs, my wgdc is high. What else can be wrong? https://bootmod3.net/log?id=69eec89ab871d247c3c5cbf6 (after cleaning BOV) https://bootmod3.net/log?id=69e5239bcb224d0c3d8d2932 (before cleaning BOV) Last edited by LIVY435IGC; Yesterday at 11:11 PM.. |
|
Appreciate
0
|
| Yesterday, 07:39 PM | #91 |
|
Major General
![]() ![]() 4658
Rep 7,981
Posts |
Targeting 23psi on stock turbo? Looks like you are maxing stock turbo... Did you expect lower WGDC with that aggressive of a tune?
I dont know enough about the turbosmart personally to comment on your leak situation. |
|
Appreciate
0
|
| Yesterday, 11:13 PM | #92 |
|
Second Lieutenant
![]() 31
Rep 200
Posts
Drives: 2015 435i Gran Coupe
Join Date: Dec 2014
Location: Plano, TX
|
Sorry I didn't include the pure 500 Turbo
|
|
Appreciate
0
|
| Today, 08:38 PM | #93 |
|
Second Lieutenant
![]() 31
Rep 200
Posts
Drives: 2015 435i Gran Coupe
Join Date: Dec 2014
Location: Plano, TX
|
Based on my datalogs, is my high wgdc indicative of a boost leak?
|
|
Appreciate
0
|
| Today, 08:43 PM | #94 |
|
Major General
![]() ![]() 4658
Rep 7,981
Posts |
I cant say definitely as i dont look at a ton of P500 logs. Your tuner should be able to tell you based on his experience tuning cars with P500s. It also looks like you are logging in 3rd and should be in 4th if 8AT. Higher load might help lower WGDC.
Unrelated, but your plug gap also seems excessively small. |
|
Appreciate
0
|
| Today, 09:35 PM | #95 | |
|
Second Lieutenant
![]() 31
Rep 200
Posts
Drives: 2015 435i Gran Coupe
Join Date: Dec 2014
Location: Plano, TX
|
Quote:
Thank you! His instructions are to do it in 3rd gear. Ill ask him about your comment about the 4th gear with the 8at |
|
|
Appreciate
0
|
Post Reply |
| Bookmarks |
|
|